My MG's Garage
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PrologueIt was a nice Saturday near the end of June. Johnny and I were putting the final touches on getting his "B" back on the ground and running. His nephew Ben offered us the use of an engine hoist, but work and family obligations had delayed him being able to get over to my Garage to pull the engine out of the TD. So Johnny and I were concentrating on getting the suspension on the red car done. Johnny's brother Tom, Ben's Dad, and an avid Model T (of the Ford persuasion) Restorer volunteered to bring an engine hoist, and help pull the engine out. Since the TD uses British Whitworth (BSW) threads I had to make some bolts for the engine stand, I bought from Northern Tool. I wanted hardened bolts at least grade 5, preferably Grade 8, but couldn't find any long enough. Graciously, Mark Brandow, owner of Quality Coaches lent me a tap and die and told me to buy 5/16th Fine thread, and re-cut them. So the stand was ready, and I was ready, tomorrow Johnny, Tom and Ben would be over and we would pull the engine. There was plenty of daylight left, and my wife was out shopping, so I decided to get the honey-do landscaping chores out of the way so I would have more time to play in the engine bay. Nothing stops a rebuild project like a Coronary, let me tell you. Needless to say, Tom, Ben, and Johnny didn't make it over that Sunday afternoon as planned. It was a month before they would even let me twirl a wrench at all, and I only wanted to pull the plugs in my "B" to check them. Back in May, Johnny and I removed most of the all the connections between the Part I -- Removing the EngineOn a nice Friday evening in the beginning of September I started taking the car apart. Following the shop manual instruction, I removed the carpeting as The next thing to be removed is the transmission tunnel cover and the prop shaft tunnel. Well Johnny showed up, and we set about to assemble the engine Part II -- the analysis and planningWell the engine was torn down into its component parts. After much thought I decided to bring the engine up to MG-TD MkII specifications. by the time I am done it while it won't be a MkII it will be a MkII 1.75. I don't think at this time I will opt for either the 4.9 rear end, or the friction shocks. Everything else will be to MkII specs. One of my other objectives is to take as little metal as possible off the engine. I plan for this to be the last time in my life to have to do this, and hopefully in the lifetime of whichever of my kids end up with this thing, in theirs as well. It looks like there is some blow-by between number 3 Cylinder and number 2. The heads, pistons tops and plugs are heavily covered with carbon, indicating a chronic over-rich mixture. The Tappets seem in good shape but will need to be re-ground. I am told that they are not using as quality material for the tappets as the originals so I am better off having them reground . The number 3 Cylinder had a lot more rust, but no pitting, probably from sitting around a lot, the SU Fuel Pump quit, but has since been fitted with new points. The diaphragm seemed in good order, and it pulls a lot of air. The previous owner put a glass pack muffler on, and thus it sounded like a truck, Mark lent me a free flow exhaust for an MGA 1600 and it seems to fit in the space available. The cam shaft bearings and cam showed some signs of wear, and will be replaced with the Moss crane version. New MG TD MkII valves have been procured, and will be installed with steel guides, and hardened seats. This will require some regrind of the combustion chambers, how much will as yet to be seen. The crank has been previously reground as it is running 0100 bearings in the big-end and mains. The reason it leaked oil so much is that the cork seals in back and the rope seals in front do not appear to be around. Also the little aluminum bracket over the rear bearing cap is missing, although the cork seal is still on the bearing cap. As you can see from the photos, the engine was painted Chevy or Massey Ferguson Orange. This will be changed to MG Red. I am considering replacing the oil filter with the Fram Spin-on replacement, and installing the Moss Seal Kit. I have not been reading great things about it on the web, but I park one MG above the other, and so it is not my garage floor that will collect the oil, but rather the "B," and that is not acceptable. So if this will cut the leakage to zero, it seems the way to go. Part III -- Engine ModificationsThe complete specifications for this engine mod was done up on an Excell spreadsheet, and will be available for download soon. Change a few of the numbers for your car, and you can figure out the effect of changes to the engine. So we begin ... The head went off to Cylinder Head Service of Minneapolis, MN (612-721-4112) for first hot dipping, and then using Non-Destructive Testing (NDT) to see if there were any cracks in the head structure itself. The head tested fine, and was totally stock, so I had Tom put in steel guides, and the valves ground out to take MKII valves. Stellite seats were put in so that using unleaded fuel is no longer an issue. A Good article on using reformulated (read that lead free) gasoline was published by the Chicagoland MG Club that goes into why you should do this. I opted for steel guides since the bronze oilite guides do not expand and contract at the same rate as the steel valves, and can bind, causing strain or even damage to the entire valve train. This was relayed to me by more than one respected source. The valves were reground to a 3 angle grind. Research showed that for the XPAG engine better airflow occurred at lower valve seat angles so the valaves were ground to a 15-30-45 degrees rather than the more conventional 30-45-60 used for modern engines. The head was collected and taken to R&R Performance (Columbia Heights, MN) where the porting and polishing was accomplished. Brian was very good to work with, and did excellent work. However this will be the last XPAG head they he wants to work on. He doesn't see very many of them, and they have decided to reject working on them since they had to create special jigging to work on the heads. He gets enough Small Block Chevy engines to work on, so they just don't want to take the extra time that the occasional XPAG engine takes. When they did return the head it the intake and exhaust ports were widened to just a fraction less than the manifold gaskets, and the ports were ground and polished heavily, but not so much that the shape or valve choke was impaired. The ports were smoothed and blended into the bowls, and pocket ported to make the airflow smooth into and out of the intake/exhaust valves. The inlet port outer stud boss was ground away about 0.060 in. to make the ports 1.1875 inches high by 0.65625 inches wide, and the "beak" behind the stud boss was polished and radiused. The net effect of these modifications were to smooth out the entire airflow to aid the XPAG in breathing in and out. This engine in my opinion is pretty well choked up, and some additional HP can be gained from this original "tractor" engine. The combustion chambers were polished but no additional metal was used. 0.0897 inches were removed from the head thickness bringing it to a finished thickness of 2.928 in. bringing the engine's compression ratio to 8.61:1. Lastly the combustion chambers were measured to confirm they were 4.5 cc's. While bringing the engine up to MarkII spec's, except for the porting and polishing, I am endeavoring to remove as little metal as necessary, yet to do the job right. The head was returned to Tom at Cylinder Head Service and the valves and Mark II valve springs were inserted. and the completed head returned. The crankshaft was sent to Crankshaft Supply (Minneapolis, MN ) where the crank was magnafluxed, polished, and ion nitrided for durability. The crank came back 0.020 under, and the correct bearings were ordered through Quality Coaches from Moss. Additionally new cam bearings, and the Crane standard grind cam and shorter rods were ordered as well. I picked up a set of used MGA HS4 1-1/2 inch Carbs and ordered the rebuild kit from Moss. More on the carb rebuild later. A free flow exhaust for an MGA was recommended by Mark to finish up the breathing package. The engine has just gone into Competition Engines (Burnsville, MN 651-688-6351). Randy is currently NDT'ing the engine, hot dipping it to clean it up, and will clean and hone the cylinders. It seems that the #3 cylinder picked up some rust, (a good justification for fogging the engine prior to putting them away for the winter, since it is highly likely that one valve will be open when the engine stops) and we quickly miked the engine and its seems to be 0.030 over bored. After the wash, and Magnaflux, Randy will mike the bores and let me know if we can get by with a 0.040 overbore. I will then be able to order the pistons, rings, gudgion pins and frost plugs for the engine. and a dynamic balance of all moving engine parts comes next. The current Tappets are slightly grooved, but Mark thinks that I can get by with resurfacing them -- we will see. That's it for now --- soon we may have an engine again rather than three boxes of parts. |
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